사력댐 침투수량 측정 시스템의 비정상 계측원인 조사 |
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학술지명 한국지반공학회
저자 이종욱
발표일 2016-03-17
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The target dam in this study release the stored water of average 22,000m3/day into the down stream river through the outlet pipe to supply an agricultural water. The downstream water level can be controlled by the water barrage built in the down stream river. Inflow into the seepage measuring house was increased from April 2012. The V-notch wier was flooded by the increased flow rate exceeding the capacity of drainage pump. The capacity of drainage pump was 60m3/hr. If the increased flow had resulted from the flow through the core zone, the possibility of severe problem on the dam stability such as internal erosion and piping of core zone could be considered but these were not questioned because the turbidity of incoming water was almost clear with maximum 2.2NTU (Nepthelometric Turbidity Unit). Another cause could be expected was the inflow of the downstream river water through the seepage collecting system. In this study, correlations among the measured seepage flow rate, the reservoir water level and the released water supply rate for agricultural are analysed and the temperature, turbidity and pH of the inflow water also measured and analysed to investigate the possibility of inflow of the river water. CCTV (closed circuit television) surveys and field investigations for the collecting pipe and seepage collecting wall and the foundation of it were carried out to find out inflow path of the river water. |